- #45 of 71
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Re: 1982 F150 Electrical Problem [dglarson]
by ckelton489
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Jun 08, 2008 (3:39 pm)
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Replying to: dglarson (May 17, 2008 5:21 am)
i would start with the steering column i too had the same prob but never acted exactly like that..just some of the stuff didnt work then not realizin it they did work but not thinkin bout it at the time....i just pulled off the steering wheel and started cleanin all the contacts. then everything worked and never had a prob since, now granted this may not fix all of ur probs but it should help alot plus theres not alot of work and its cheap to do.
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- #46 of 71
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'85 F-150 smog pump
by ckelton489
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Jun 08, 2008 (3:46 pm)
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i just put dropped in an all roller 302 fuel injected...which i converted to carb. i installed all new exhust startin with long tube headers and true dual all the way back... i even put in 2 cats for each pipe the truck is quiet id like to have some noise but thats not the issue...i just got pulled over the other day for expired state inspection sticker. i do not have it inspected cause im not sure if i would pass with no smog pump....theres nothin to hook it up to....so does anybody kno what i should do? i didnt get a ticket this time but dont mean i wont. so i need to do somethin soon. i will try next week but im pretty sure of the answer.
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- #47 of 71
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Re: HELP Please [noooobie]
by ckelton489
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Jun 08, 2008 (3:55 pm)
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Replying to: noooobie (Apr 19, 2006 8:06 am)
alrighty bub ur carb needs to be adjusted...the needle and seat aint lettin the fuel into the bowl so its usin the fuel in the bowl till it runs out so the needle and seat aint openin up enough to keep fillin it back up...it should actually stay at one level continuously just adjust that as its runnin till its right...lemme ask is it a holley? they are famous for that and unfortunatly u'll be adjustin it alot...not now but in the future the next time u start it when its cold....and when u get it runnin cont. u'll still have to adjust it then....its tedious i mean u can onlt turn it like 1/32 of an inch at a time till it runs right on and off the throttle...if its a4bbl u'll have 2 bowls 2 needle and seats. front and back right there on top
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- #48 of 71
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Re: 1960 Ford F100 [tweetybyrd505]
by mike9408
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Jun 20, 2008 (8:06 am)
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Replying to: tweetybyrd505 (Jun 27, 2007 9:22 pm)
Hi Tweetybird,
Many of the starters produced require a strap (usually copper) which goes under the Battery Positive lead to the solinoid terminal. This supplies power to the ignition system complete and provides power to the solonoid. Without this strap nothing will work (other than jump starting as you have indicated. Install the strap should solve your problem. Mike9408
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- #49 of 71
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Re: F100 Negative Coil Wire [kjmac1]
by mike9408
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Jun 20, 2008 (8:27 am)
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Replying to: kjmac1 (Oct 31, 2006 7:43 am)
I realise this is an old posting but to clear it up for anyone else out there...The Positive side of the coil comes from the ignition switch (when you turn the switch on it sends power to the coil). The negative side of the coil (while it may appear to go inside the cab) eventually ends up connecting to the Distributer. If you run this wire to a common ground you will either burn up the wiring or burn a fuseable link somewhere in the system. Good luck.
Mike9408
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- #50 of 71
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Ford 302 Miss
by crabmanlan
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Jun 27, 2008 (8:51 am)
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My 86 Ford F250 302 TBI has developed a hard "miss" upon accelleration. It runs well at idle, at any speed reached by slow accelleration but upon hard accelleration as in passing or on a steep hill it missess hard like no fuel or no spark. It will continue to do so until you let off. There is occasionally a Pop.
Any thoughts?
Lanny
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- #51 of 71
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Re: My '85 F-150 won't accelerate normally [trobertc]
by csnover
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Aug 03, 2008 (7:56 pm)
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Replying to: trobertc (Jun 03, 2008 10:56 am)
I'm guessing you have fixed this problem by now but if not...When I had my 87 ford and I would try to floor it the same thing happened. What I found was that I was sucking in air from my exhaust manifold because of two cracks around where the carb connected in.
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- #52 of 71
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1977 ford simple problems
by csnover
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Aug 03, 2008 (8:09 pm)
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I just bought a 1977 Ford 150 and the last owner put an after market steering wheel on and after I bought it I realized that the blinker swtich on the steering column just hangs loose. I was wondering what it connects to inside there to keep the tension on it so you can switch the blinkers on and off. I haven't had time to take it apart yet
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- #53 of 71
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Re: 1987 F150 4.9l 4x4 4spd man [trobertc]
by asaley
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Aug 06, 2008 (5:56 am)
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Replying to: trobertc (Jun 03, 2008 10:45 am)
You may have trash in your tank. I had about the same problem several years ago after we had the gas shortage (9-11). I would be going down the road and seem to run out of fuel but with plenty left. I ended up pulling the tank and cleaned out a lot of junk . I changed the strainer and filters. I think I got it when I filled up while the were receiving a truck load into a almost empty tank which sturred up the bottom and I got a lot in my tank.
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- #54 of 71
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64 f 100
by rford302
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Aug 10, 2008 (8:48 pm)
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how do i figure ot where to position a cross member motor mount for a 302 on the frame rails???
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